Sunday 10 November 2013

Fabricating New Vulliamy Pallets for a Vienna Regulator Clock

I'd like to thank David La Bounty for his invaluable technical advice and Ken Simmons for the use and support with his industrial size lathe to machine the original piece of tool steel. My clock maker lathes were simply not big enough to perform the original cut!
The wear on the original pallets can be clearly seen in the picture below. Ordinarily it might be possible to grind and polish the impulse faces, and refit. However I think these have had that done before now, as they are quite short, leaving little room to remove enough steel to give a clean face.  Unfortunately the existing ones are not reversible; i.e. where the pallet can be turned and fitted in the opposite verge arm, as both ends have been ground. So completely new pallets required making. This will mean that a complete ring will need to be made in order to ensure that the curvature of the nibs is as required, and the nibs then cut out of the completed ring.
In picture 1 the 60mm tool steel rod can be seem in the lathe chuck. It is quite a piece of steel given how small the pallet nibs will be. The outside diameter of the ring required is ascertained from measurements already known, i.e. the distance from the centre of the verge arbor, to the outer edge of one of the existing pallets = 51.68mm.

The inside diameter is taken from the Outside diameter minus the thickness of the pallet nib required.
= 51.68mm – 0.94mm = 50.74mm

The outside diameter is cut first and polished whilst on the lathe, not just for convenience, as the thickness of the ring can then be measured as the boring out of the internal diameter actually progresses (picture 2), using the outside finished and polished diameter as a constant, given there will be no further material removed from the outer diameter.
In picture 3  the ring can be seen to just beginning to locate in the verge. This was enough of a cut for now, as any surplus material on the internal diameter would be taken off in a polishing process.
There was a good amount of chatter when commencing parting off the ring from the steel rod, despite the tool being very sharp and central, and kept close to the tool post. So I adjusted the cutting tool to give a slightly negative cutting rake, i.e. the cutting edge was sloping downward by a degree or two. The parting tool was also ground with a slight rake across its width in order that the cutting edge (on the right edge) meant the ring parted from the rod with very clean edge. The tool adjustments made quite a difference and parting off was clean.

In picture 4  the ring can be seen to be mounted in a small chuck on my Lorch 6mm lathe, the jaws have been reversed to accommodate it. However holding the ring too tightly ran the risk of distorting it, so small pieces of thick double sided tape were used to hold it in situ, whilst the jaws were minimally tightened. Round wooden dowling was used, loaded with emery paper, to polish the Internal diameter. From 600grit through to 7000grit, in stages. 


Picture 5  shows the completed ring sitting snugly in both slots in the verge. Clamping the ring between two thin pieces of wood (Picture 7) in a vice gave support for cutting lengths off to make the nibs. This ensured that the jewellers scroll blade did not ‘skip’ across its polished face, undoing all the polishing work. It also held the cut length in situ until the blade was all the way through, ensuring a very clean cut. 


Picture 6 shows the jig I made to hold the verge during the process of grinding and polishing the impulse faces on the nibs. This could  be mounted on the cross slide of my Lorch lathe. The verge must be able to ‘swing’ on a constant axis point onto the face of the grinding and polishing wheels, yet still be held firmly in order to discourage any chatter. I used a modified old centre wheel spider spring for applying tension onto the brass disc holding the verge to the aluminium plate. Hence the tension was adjustable. The brass disc was turned to have a radius of exactly half that of the measurement between the centre of the verge arbor and the dead centre of the pallet nib. This measurement meant that a tangent line from the edge of the brass disc could be aligned with the face of the grinding and polishing wheels, ensuring an impulse face of 2° would be ground/polished, picture 8 and 9. 



                                          

 Picture 11 shows the exit side pallet being ground, and the tangent line mentioned earlier. The brass wheel in picture 9 was made for sticking the emery paper onto for finer grinding and polishing. Once the brass wheel’s desired diameter was cut, its front and back was faced off on the lathe to ensure it turned square and flat to the pallet nibs impulse face. If it does not run square and true the impulse face could be ‘buffeted’ by the wheel and lead to a lesser finish. After using the grinding wheel for removing the initial amount of steel, I used cut discs of emery paper, stuck to the brass wheel with a spray glue. It does not take much glue to stick these on satisfactorily.
When using the emery paper on the brass wheel, once the face has been ground on that grade, moving the pallet nib impulse face slowly across the paper using the cross slide, whilst keeping light pressure on it with my finger, effectively removes any lines left by the paper. This is especially effective during the last polish. Grades of paper used in sequence were grits 600, 1000, 1200, 2500, 3000, 5000, 7000.
It’s a good idea to check your tangent line after changing the grade of paper, given they differ in thickness.

Pictures 10 and 12  show the finished pallet nibs, with clean edges and even impulse faces. They are hardened by heating to cherry red and quenched, followed by tempering to very light straw colour and quenched again. Followed by a final impulse face polish on the jig set up, polish of the locking face with 7000grit, and finally polished using a felt buffer and a super finish polishing compound.   

                                                                              
                           

Saturday 3 August 2013

Fabricating a Replacement Pendulum Hanger

The movement for which this was fabricated was made by M Bauerle ca1925 and is of a very high quality. A 'make do' pendulum hanger was being used, however having serviced and repaired the movement I was keen to ensure it was restored to as an original state as possible. Finding an original brass pendulum hanger was not going to be likely at all. Thankfully a fellow friend in horology had the same movement and kindly forwarded details of the pendulum hanger on his movement (first pic below). The first piece to be made was turned on a watchmakers lathe, using a hand held graver (second pic). This part would have the pendulum leader's hooks over its spokes.

           

3mm brass rod was used for the hanger's length; 5mm brass rod for fabrication of the hangers top hook, the section that sits between the crutch forks and the lower part where the pendulum is actually hung. The first pic below shows the nearly completed bottom section of the hanger and the section that sits between the crutch forks. The second picture shows the early stages of the hanger's hook fabrication. The only part of the hook worked in the lathe was the tapered end, which also had a 3mm hole drilled through it in order to receive the 3mm brass rod.



The hook was shaped and formed by hand using a jewellers hand scroll saw and very fine files. The final finish to all parts was achieved with P7000 grit wet and dry paper.

                      


The pictures below show the bottom part of the hanger ready to take the pendulum, and the completed unit ready for fitting to the movement.







       

Monday 29 July 2013

Longcase Clock Movement ca1830. Service and Repair.

This is a typical movement of the period. Many of these movements were made in foundries as 'kit form' and sold to clock makers. Though it required a great deal of skill to produce a working movement.     

There was a great deal of wear through out the movement. Notably the pivots showed significant wear, beyond what could be rectified by re-facing and burnishing. Below are a few examples.

      
           

Six pivots were found to require replacing. The worn pivots were cut away and new holes centred and drilled into the ends of the arbours. Followed by new pivot steel fitted into the holes, faced, polished and burnished. The picture below shows a repaired pivot.


Every pivot hole in the movement plates required attention, worn over time by the rotating pivots. The first picture below shows marks on one of the movement plates highlighting what side of the pivot holes are worn. Before a brass bushing can be fitted in these to make good the wear, the holes must be re-centred and reamed out. Accurate re-centring ensures that the wheels and pinions engage by the correct depth.  The second picture below shows a centred and reamed hole in the plate ready to accept the new bushing for the main wheel arbour. 


                      

The main wheel arbours are the largest in the movement and bear the weight of the 12lb lead weights. The bushings need to be a tight tapered from the inside, and be peened, see first picture below, into a slight chamfer  the newly reamed hole to prevent them shifting out of the hole, especially during winding of the movement. Following this it can be filed flat and finished in order to make the finish the repair to a high quality and original condition.

               


The first picture below shows the re-bushed strike train. All wheels are able to turn freely and engage at the correct depth. The same work was carried out for the going (time) train. Other pictures show the movement restoration complete and ready for testing for two weeks before being fitted back into the clock longcase.